Projects
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Aloha
32 Rudder Post & Steering Rebuild (1)
by
David Querbach
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We've just finished
a complete rebuild of the steering system on our Aloha 32. When we
purchased the boat in November 2005, we noticed about 1/8" play in
the top rudder bearing. After hauling the boat, we also noticed
about 1/16" play in the bottom bearing.
Upon pulling the engine for repair, we found about 1/2 gallon of sandy
sludge on top of the quadrant, on the hull around the rudder post, under
the fuel tank and engine, and on down into the bilge.
We disassembled the steering system to investigate. I'll describe
the construction of the steering system in detail, because I think it will
help in discussing the problems and the solutions we chose:
As built, the rudder shaft is a 1 7/8" OD stainless tube. Near
the top of the shaft is a 1/2" diameter stainless pin inserted
through the diameter of the shaft. Under this are two 4" diameter,
1/2" thick aluminum disks. The 1/2" rod is secured to the
upper disk with a stainless machine screw. The lower disk rides on a
plastic bushing which looks a bit like an inverted top hat.
A 1" deep drain well extends across the width of the cockpit sole
with drains in the outboard corners. The "brim" of the
rudder bushing rests on the floor of this well at the center, with
the tubular part extending down through a hole in the floor of the drain
well. The "brim" of the bushing is secured to the drain
well floor with three 1/2" flat-head wood screws.
We found that the bushing, and thus the entire shaft assembly, was moving laterally
at least 1/8" inch when under load. The bushing was also
rotating about +/- 10 degrees when the rudder shaft rotated. The
screw holes were elongated, so the screws were no longer doing their job,
and in fact their heads were gouging out the bottom of the lower aluminum
disk.
It's clear that the sand and grit, carried by water from the cockpit sole,
migrated underneath the bushing, onto the quadrant, and thus down into the
bilge. In fact, the sand underneath the rotating bushing milled
down through the fiberglass into the plywood.
Our lower rudder bearing is a simple fiberglass tube. Over the 22
years since our boat was built, the rudder shaft was worn down about
.003" in diameter (as compared to the unworn parts of the shaft).
The tube was about .060" larger in diameter than the shaft.
Unlike some other sailboats, there is no packing gland at the top of the
rudder tube. The top of the tube appears to be somewhere between
3" to 5" above the static water line, so when the boat was new,
the close fit between the tube and the rudder shaft presumably kept the
water out, even when under way.
It's interesting to note that another Aloha 32 owner recently reported
leaking from the front of his rudder tube at high propeller speeds.
We only had a few hours on our boat before we hauled it for refitting, so
we didn't observe any leaking. (But with the mess in the aft space
of our boat, it might have been difficult to see in any case.)
The quadrant on our Aloha 32 is actually a complete wheel, and is clamped
with several bolts, and secured from rotating with a pinning bolt through
the shaft. When we removed the quadrant (luckily it was easier for
us than for you), we found the bottom of the quadrant severely eroded, to
the point where the pinning bolt was exposed over most of its length.
The rim was also quite rough from corrosion.
Since the quadrant was mounted only about 1/8" above the top of the
rudder tube, one imagines that water splashed up the rudder tube onto the
bottom of the quadrant from time to time. The quadrant, being
aluminum and anodic with respect to the stainless shaft, eroded away.
Here's what we did
to solve the various problems:
Bottom Bearing
After considerable research, we decided to rebuild the bearing surface by
injecting graphite-loaded epoxy into the rudder tube, using the rudder
stock as a mold. This method is described in section 8.4 of
"Fiberglass Boat Repair & Maintenance", published by West
System Inc.
In short, the technique is to remove the rudder, drill several holes into
the rudder tube, reinsert the rudder, then use a syringe to pump
graphite-loaded epoxy through the holes into the gap between the rudder
stock and the rudder tube.
To begin, we dropped the rudder and cleaned up the shaft with coarse emery
paper. We especially concentrated on working down the unworn parts
of the shaft to try to eliminate the .003" step worn by the rudder
tube. We were concerned that since the new bearing diameter
would be based on the lower, worn part of the shaft, the upper, unworn
part of the shaft might not fit through the bearing when we needed to
remove and reinsert the rudder.
Next, we drilled four holes in the skeg from outside the hull, diagonal to
the boat's centerline, and parallel with the waterline. We
originally hoped to find solid fiberglass here, but we found an air gap
between the skeg and the rudder tube. While it might be possible to
fill this gap with a low-viscosity epoxy, we decided to simply find a syringe with a longer
nose. We ended up drilling 1/4" holes right through the rudder tube,
and 3/8" clearance holes in the skeg to provide clearance for the
syringe nose.
We then applied two
coats of mold-release wax to the rudder stock and inserted the stock into
the rudder tube, blocking the shaft so it was approximately centered in
the tube.
Following the instructions in the West System book, we created a 50/50
mixture of graphite powder and colloidal silica. (The graphite power
adds strength, hardness, and lubrication to the completed bearing surface;
the colloidal silica is a thickening agent.) We added this mixture
to some System Three epoxy to get a mayonnaise consistency, and
loaded the result into a syringe.
The West System instructions suggest injecting only enough epoxy to form
1" diameter pads inside the rudder tube. We instead injected
enough epoxy to form a 2" to 4" band all around the tube, since
we wanted to form a barrier to water coming up the tube. Using a bit
of simple geometry, we determined that 20 ml should be about right, so we
injected about 5 to 7 ml into each of the four holes.
It's important that the syringe fit tightly into the hole in the rudder
tube, since you need to apply significant pressure to get the epoxy to
flow inside the tube. We had one hole that didn't fit well, so the
epoxy squeezed out past the syringe. The resulting bearing surface
at that point was only about 2" high, rather than the 4" of the
rest of the bearing. Next time, I'd epoxy the bad hole and re-drill
to get a better fit before injecting.
While injecting, we could tell that the epoxy was flowing as desired, and
that our calculations were correct, because we could see the epoxy show up
at the holes on either side of the first holes we injected into.
We let the epoxy cure
for about eight hours, then turned the rudder to break it free, and then
came back every few hours to break it free again. We left the rudder
in position for about a week to ensure the epoxy was completely set.
We wanted to avoid damaging the new bearing surface when we dropped the
rudder for the rest of the required repairs.
Top Bearing
While the bottom bearing was curing, we set to work on the top bearing.
Since we had hammered pretty hard on the top of the rudder shaft to get
the aluminum disks off, the floor of the drain well, which was already
damaged by the sand milling away the fiberglass, was now delaminated as
well. To begin the repair, we ground away the loose fiberglass and
wet wood over an area about 8" square. We then used System
Three RotFix (a penetrating epoxy) to stabilize the wood and secure the
remaining fiberglass to the wood. Finally, we laminated back up to
the original thickness with epoxy and glass cloth.
We wanted to make sure that any water and grit in the drain well would
drain away from the rudder bearing in the future, so we added a 1/2"
thick plywood land under the rudder bearing, beveling the edges and
glassing it over. On reassembly, we omitted one of the two 1/2"
thick aluminum disks to maintain the original rudder shaft height.
We eliminated the possibility of water in the plywood by drilling the hole
for the bushing about 1/4" oversize, which allowed space to pack in
epoxy loaded with milled fiber around the bushing.
To ensure a really accurate fit of the epoxy around the bushing, we used
the bushing itself as a mold. We first applied a generous coat of
mold-release wax to the bushing, then we dropped the rudder a few inches,
inverted the bushing and put it on the shaft. We raised the rudder
back into position, pushed the bushing up until it met the bottom of
the drain well, and secured
it there with duct tape. It was then possible to pack in the epoxy
and milled fiber around the bushing. We let the epoxy cure well,
then removed the bushing.
Once the hole was cleaned out and the bushing reinserted from the top, it
was perfectly aligned with the shaft and had absolutely no slop
whatsoever. Finally, we drilled for the bushing retaining screws.
Again, we avoided any future water ingress by drilling a bit oversized,
packing the holes with epoxy and milled fiber, and re-drilling for the
screws after the epoxy cured.
Quadrant
Even though the rebuilt bottom bearing should exclude water for some
years, we wanted to avoid having to replace the quadrant ever again.
The Edson radial drive wheel used on the Aloha 32 is shaped like a shallow
dish, with a hub on the bottom of the dish. As built, the wheel is
mounted dish up, with the hub below. After much careful measuring,
we determined that there is enough vertical space below the drain well to
mount the quadrant upside-down. The inverted position puts the hub
above, with the
dish facing down.
According to the Edson manual, this mounting arrangement is completely
acceptable, as long as the cable runs true onto the rim of the wheel.
Mounted in this way, the quadrant is several inches above the top of the
rudder tube, so that any small amount of water which may intrude will not
be able to reach it. Another advantage is that the quadrant clamping
bolts are now on the top, so are easily accessible from the lazarette for
the next time we need to drop the rudder.
Final Assembly
When reassembling the steering system, we lubricated both the upper and
lower shaft bearings, the idler bearings, and the steering wheel bearings
with Teflon grease. On the advice of our mechanic, we also
lubricated all bolts and the quadrant-to-shaft interface with the same
grease, to help avoid avoid them seizing in the future.
With a new cable assembly, a complete re-bedding of the steering column,
and a bit of paint, we figure that with a little luck we're now ready for
another twenty years!
Last
updated 07 May, 2006
- © Aloha Owners Association
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